Datalogs of the problem showed that the AFR was like a sine wave with the peak at 22:1! I suspected that this was either down to:
-Dodgy readings from the wideband itself, causing the closed loop system to go bananas.
-Problems with the black box that controls the closed loop.
-Problem with the stepper motor not doing what it was supposed to.
I disabled the closed loop, and went back to no automatic mixture control, life was good, but expensive.
I took some more datalogs of the problem through my Megasquirt (controlling ignition only at the mo) with the car running open loop but the wideband in and sniffing exhaust. These still showed some degree of bouncing AFR's with the readings moving up and down by a whole integer value or more.
I would have suspected noise to be the culprit, but the MS and LC1 are powered and earthed at the same locations (bus bars in the battery box) and the MS is perfectly happy- no resets etc. Also the period of the sine wave seemed to be around 1 second, too slow for noise surely?
Screenshots here:
http://forums.lr4x4.com/index.php?showtopic=70067
Next up I decided to lashup the LC1 so that it was powered from a couple of 3S (11.1V) Lipo batteries that I have for my various radio controlled toys. These were wired in parallel, each rated at 2200mah with burst discharge rates of up to 50C. The LC1 was therefore fully independent of the 90's electrical system.
The downside to this was that I could not log from squirt as the potential differences involved between LC1 and MS would give me problems. I am therefore stuck with working only with the logworks files, which give no indication of load, rpm etc.
I took these logs this afternoon- I still think that they are too spiky. And at one point the gauge went berserk, again bouncing from rich to massively lean with the car showing no undue effects- i put this down to a problem with the readings, and not an actual problem with the mixtures.
So- can someone take a look at these and tell me if they think they look bad? Apologies for the rubbish file host- I hope they download ok.
You will need logworks to view them.
Engine running (I stopped for LPG at one point with the LC1 still powered, engine off):
http://www.filedropper.com/lipos
Engine switched off (looks good at the start but gets progressively worse):
http://www.filedropper.com/engineoff
I even tried covering the tip of the exhaust on this one to try an negate any impact of the wind blowing.
I have also tried multiple free air calibrations, and heater calibrations, all with the same results.
So the big question is this- do these look normal to you? (ignoring the actual AFR's and focusing on the consistency of readings for now)
Thanks in advance
Jamie





